BensonHsu.com

previously the sileightymania.com journal.

Browsing Posts published in April, 2003

Clutch gone

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Video of me from the last journal entry: here

Well, my clutch went out… so Cartune put my old one back in along with a kouki 180 transmission. That transmission is bad, and leaking everywhere. Hahah. What luck I have. Air in my clutch lines decided to totally keep me from driving also – so Alex and Marc came over to help me late on Sunday night so that I could drive to work. Thanks guys! We concluded that all of the air was the result of Nissan’s use of a clutch line dampener right before the clutch line to the clutch slave cylinder – It’s not made to make bleeding the clutch a very easy job. So basically we removed it. And we bled it, and now everything is fine! I’m trying to get hold of a new clutch… maybe Exedy if life is good to me. In other news, I’ve got new anti-sway bars! I drove down to Torrance last weekend and installed a set of Tanabe anti-sway bars… they are noticibly larger than the stock bars. On the way home, I could feel it right away – even while driving out of the parking lot. Turning feels a lot more solid ESPECIALLY at speeds over 20mph. It was amazing how much of a difference it made while just driving on a banked freeway interchange! I really suggest that, when you get the money, to invest in some. I’m loving these. Anyone going to SEMA International Auto Salon? I think I’m gonna go see what’s going on over there. Ooh, Ray from KAAZ USA told me that I’m in this month’s HCI and LA Auto Weekly. Time to go magazine hunting! Drive safe everybody!

Sorry for leaving you all hanging! The engine is now running GREAT… it wasn’t a boost leak afterall… the wiring to the MAFS was falling apart, and it caused the car to idle fine… but the power wasn’t there. After fixing that, the engine is running STRONG. I mean, the car pulls really hard, and if I put the car into 2nd from 1st gear aggressively, the car will start fishtailing and will spin the rear tires for a while – with 215 Bridgestone S-03 on the rear!! There is still a small whining that is in tune with the rpms… I originally thought it was a loose spring on my clutch plate, but since I changed the clutch and the sound is still there, I’ve concluded that it’s something in my transmission. Good thing I got a transmission with my new engine!

The RS-R Drift Festival was great… again, Club4AG has raised the bar, and again, the US drifters stepped up to it. I can’t believe what a great show some of our drivers can put on for the crowd. I heard lots of cheering… as if this was a “real” driving event! It was great. So here’s my story… I started out with a new engine and new tires on the rears… I figured that I would try using my 215 Bridgestone S-03s on the rear – I didn’t like it. I had 3 laps to figure out my new setup… and I just could not predict the tires, maybe because I just need more time figuring out a rear sticky tire. I’m not sure, but I changed them after my first 3-lap session. The 2nd 3-lap session came around when suddenly I realized that my clutch went out on my 2nd lap. D’OH! I thought my day was over.. I brought my car back into the KAAZ booth, feeling kinda sad that I wouldn’t be able to drive for the rest of the day. Richard (JDM RICE) was nice enough to offer me his car for the competition (the next round was the start of the competition). Thank you Richard! My competing mentality was pretty much over for the day, since my car went bye-bye, but I figured that I could still have fun. So I went out… we had 2 laps to compete, which meant I had 2 laps to figure out his 330hp monster – with 275 wide tires in the rear. Needless to say, I couldn’t figure out the car in 2 laps Hahaha. But I did get a lot closer with each lap… it’s hard trying to drift while trying to overcome a handicap (boost lag under 4000rpms). But I am proud of myself for drifting the high-speed back sweeper… I started the slide in the top of 3rd gear and brought it all the way around to connect to turn 1. That in itself was a big accomplishment for me. Richard’s car is like a challenge for me now… I hope he’ll let me drive it again soon :) That’s the end of my story… congratulations to Alex Pfieffer, Andy Yen, and Ernie Fixmer for doing a GREAT job!! You guys are bad-ass! I saw A LOT of other people out there doing great too… you guys are bad-ass too! haha! Keep practicing… keep pushing the limit… and keep having fun and making friends!

New Engine

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As of today, there are 3 days left before the RS-R drifting event, and my car isn’t ready. What else is new?? Last weekend, Cartune helped me out and put a kouki 180sx engine in my car… But since then, my clutch master cylinder has needed replacing, and now there’s a boost leak that we can’t find. Tuesday night, after changing my LSD oil at KAAZ, Neen, Kris, and I went to go eat in Costa Mesa… then I found out that some JERK in the parking lot hit my car hard, and completely crumpled my fender! And took off without leaving a note! Things like this remind me what complete jerks there are out there… and it’s also a reminder for me that I need to be a good honest person so that I don’t anger people the way that I was angered from my newly crumpled fender. Ahh, I guess it doesn’t matter – what can I do? Bang it out with a fender and pretend it’s not there! Well, I’m gonna go work on my car right now and try to find out how all my power is leaking out of some place. Wish me luck… I’ll see you guys on Sunday!